SupraSean;1627114 said:Sorry guys, have been uber busy,,,,, ok so with boost leaks still, a shitty tune and 5 psi, i made 258 and 262 trq. sadly i couldnt keep it to hold 10psi, so im guessing it was somewhere between 7-10 and made 300 flat with 278 trq, now heres the kicker. we ran it to 6k, it was still climbing VERY steadily. no drop off at 6k. so the turbo is definately performing well, especially being that its barely waking up. i appologize for still not fixing the leaks lol but it should give you an idea. i have two more couplers to replace, i want to give her a tittie bit more pload and try again. im wondering if it wont hold boost because of the mentioned weak wgate spring. i suppose we will have to find out. im going to ask the guys at the shop to send an email with the dyno sheets so i can post them up. Oh yea, and this was on a mustang dyno, which i hear read low. just fyi
Looks promising got a graph? Numbers are higher than mine at those levels! get it fixed and get some video's!
My cooler pipes are welded up now (hot side) just need a few a silicon reducer before i start to play with the actuator again, Hopefully we can find a suitable replacement and test it that will hold high boost.