i realized my coolant resivour was full and overflowing, so i figured a blew a headgasket. i took the car to school to do a compression test to make sure it was a headgasket and i got 150-160 across the board. alright, thats good..but why is my tank overflowing. then i started thinking. well, i have my heater core valve thing bypassed..and the plastic coupler i had coupling the 2 coolant hoses together burst exploded crushed last thursday, easy fix..removed what it thought was all the pieces of the coupler..i dunno...so my thought is maybe a piece of that plastic coupler went through the coolant line and is lodged somewhere creating higher pressure. Am i thinking clearly?
Now, after we reassembled after the compression test, we realized it was misfiring. We checked everything over many times, but couldnt get it to run right. i looked the plug order on the alldata just to make sure, and it told me that the one the last coil...i had 2 and 5 reversed...thing is..i have it marked like that, and thats how its been running. flipping it made little difference. what can be wrong here any ideas?
Now, after we reassembled after the compression test, we realized it was misfiring. We checked everything over many times, but couldnt get it to run right. i looked the plug order on the alldata just to make sure, and it told me that the one the last coil...i had 2 and 5 reversed...thing is..i have it marked like that, and thats how its been running. flipping it made little difference. what can be wrong here any ideas?