Hello Supramania,
About I year ago I posted this thread in an attempt to get advice solving a problem I'd been having with an aftermarket T4 PT6262 turbo I had just installed. A year later I find myself still in the same situation. I've come back after trying several more tests/fixes in a last-ditch effort to come up with some ideas on what could be wrong. I'm afraid I'm at my wit's end now, and this may be the end of my Mk3 Supra romance if I can't figure it out.
Recap:
(Changes and additions since my last post are in italics)
Problem & Symptoms:
Manifold pressure builds to only 0-10 kPa (0-1.45 psi) at ~2500 RPM and holds until 4k+ RPM where it will rise again to only ~30-40 kPa (4.35 - 5.8) psi. No noticeable engine stumbling or roughness. The car burns a bit of oil when starting after sitting for a while, but clears up after the initial puff. It does seem to use a lot of coolant and the exhaust is a bit steamy, but nothing excessive, oil changes looked good, coolant flushes looked clean, and compression checks have turned out OK (so I'm hoping there's no BHG). I have been dealing with a stubborn CPS connector (replaced the female end, but still occasionally have trouble on start up in hot weather).
The Car & mods:
1988 Supra Turbo (7M-GTE)
R154 Transmission (auto to manual W58 done by previous owner, W58 to R154 done by myself)
DriftMotion Remote Oil Filter Relocation Kit
Apexi Power intake
V8 Lexus AFM
DriftMotion intercooler kit (includes 2.5" aluminum piping fabricated by DriftMotion, HKS knockoff BoV, 3" aluminum core intercooler)
550cc RC injectors
DriftMotion Aeromotive Fuel Pressure Regulator Kit (including steel braided fuel lines prepared by DriftMotion)
Walbro 255 LPH High Pressure fuel pump
DriftMotion Turbo kit (PT6262 turbo; .84 AR) (includes welded T4 tube manifold, HKS knockoff wastegate, turbo, turbo coolant bypass hose, oil feed line, oil drain line & flange, & 3" downpipe)
Magnaflow high-flow cat
HKS Super Dragger cat-back exhaust
EGR Delete (done by previous owner, appears to have correctly blocked off the intake & exhaust with flanges and removed the cooler plate from the back of the block)
PCV Removed (valve cover now venting directly to atmosphere, accordion hose and intake blocked off)
Aftermarket Defi Boost Gauge, EGT gauge, AEM UEGO (probe not yet re-installed in downpipe)
Troubleshooting Already Performed
Boost Leak Testing: I've pressurized the entire intake system (from turbo inlet through to the engine, with the BoV still hooked up) to ~ 25 psi and have negligible pressure loss (after blocking off the PCV pipe)
Pre-turbo Exhaust Leak Testing: Since my last post I've purchased a brand new exhaust manifold (one that wasn't molested by my questionable welding skills/cheap MIG welder) and pressure tested the system with the wastegate and turbo installed and torqued down. I did this by blocking off the manifold<->block flange with .75" plexiglass (re-used the old gasket), and duct taping my boost leak tester to the exhaust outlet of the turbine housing. No leaks (except for a bit from the duct tape and a tiny amount getting past the wastegate).
Wastegate Function Testing: In addition to the exhaust leak testing, I applied pressurized air to the referance tube to the wastegate. It cracked open at 10 psi, and fully open at ~15 psi, which is to be expected for a 14 psi rated spring.
Exhaust Blockage Testing: Checked the backpressure in the exhaust by hooking up a pressure gauge were the wideband O2 sensor fits into the downpipe. While idleing/free-revving there was no backpressure. I've also run the car down the street with the entire exhaust removed after the downpipe with no improvement in boost.
Missing Cylinder Testing: I've dripped water on each manifold runner to check and make sure they were hot after only a couple minutes of idle. All runners were hot (and presumably all cylinders functional).
Compression Testing: Previous compression tests showed good for all cylinders.
Engine Codes: none
As I mentioned I'm at my wit's end and desperate for potential solutions. Is it possible there could be some magical timing issue where the car runs fine but boost is retarded? Or some other issue with the engine itself that would inhibit the turbo from spooling, but otherwise appear to run quite well? I'm fairly certain it's not some sort of air/exhaust flow problem at this point. After a year of trying to solve this I'm about ready to give up on my Supra (even after all the work I've put into it). The only thing stopping me is that there has to be some sort of logical reason why it's doing this.
Please help!!
Thanks,
Jon
About I year ago I posted this thread in an attempt to get advice solving a problem I'd been having with an aftermarket T4 PT6262 turbo I had just installed. A year later I find myself still in the same situation. I've come back after trying several more tests/fixes in a last-ditch effort to come up with some ideas on what could be wrong. I'm afraid I'm at my wit's end now, and this may be the end of my Mk3 Supra romance if I can't figure it out.
Recap:
(Changes and additions since my last post are in italics)
Problem & Symptoms:
Manifold pressure builds to only 0-10 kPa (0-1.45 psi) at ~2500 RPM and holds until 4k+ RPM where it will rise again to only ~30-40 kPa (4.35 - 5.8) psi. No noticeable engine stumbling or roughness. The car burns a bit of oil when starting after sitting for a while, but clears up after the initial puff. It does seem to use a lot of coolant and the exhaust is a bit steamy, but nothing excessive, oil changes looked good, coolant flushes looked clean, and compression checks have turned out OK (so I'm hoping there's no BHG). I have been dealing with a stubborn CPS connector (replaced the female end, but still occasionally have trouble on start up in hot weather).
The Car & mods:
1988 Supra Turbo (7M-GTE)
R154 Transmission (auto to manual W58 done by previous owner, W58 to R154 done by myself)
DriftMotion Remote Oil Filter Relocation Kit
Apexi Power intake
V8 Lexus AFM
DriftMotion intercooler kit (includes 2.5" aluminum piping fabricated by DriftMotion, HKS knockoff BoV, 3" aluminum core intercooler)
550cc RC injectors
DriftMotion Aeromotive Fuel Pressure Regulator Kit (including steel braided fuel lines prepared by DriftMotion)
Walbro 255 LPH High Pressure fuel pump
DriftMotion Turbo kit (PT6262 turbo; .84 AR) (includes welded T4 tube manifold, HKS knockoff wastegate, turbo, turbo coolant bypass hose, oil feed line, oil drain line & flange, & 3" downpipe)
Magnaflow high-flow cat
HKS Super Dragger cat-back exhaust
EGR Delete (done by previous owner, appears to have correctly blocked off the intake & exhaust with flanges and removed the cooler plate from the back of the block)
PCV Removed (valve cover now venting directly to atmosphere, accordion hose and intake blocked off)
Aftermarket Defi Boost Gauge, EGT gauge, AEM UEGO (probe not yet re-installed in downpipe)
Troubleshooting Already Performed
Boost Leak Testing: I've pressurized the entire intake system (from turbo inlet through to the engine, with the BoV still hooked up) to ~ 25 psi and have negligible pressure loss (after blocking off the PCV pipe)
Pre-turbo Exhaust Leak Testing: Since my last post I've purchased a brand new exhaust manifold (one that wasn't molested by my questionable welding skills/cheap MIG welder) and pressure tested the system with the wastegate and turbo installed and torqued down. I did this by blocking off the manifold<->block flange with .75" plexiglass (re-used the old gasket), and duct taping my boost leak tester to the exhaust outlet of the turbine housing. No leaks (except for a bit from the duct tape and a tiny amount getting past the wastegate).
Wastegate Function Testing: In addition to the exhaust leak testing, I applied pressurized air to the referance tube to the wastegate. It cracked open at 10 psi, and fully open at ~15 psi, which is to be expected for a 14 psi rated spring.
Exhaust Blockage Testing: Checked the backpressure in the exhaust by hooking up a pressure gauge were the wideband O2 sensor fits into the downpipe. While idleing/free-revving there was no backpressure. I've also run the car down the street with the entire exhaust removed after the downpipe with no improvement in boost.
Missing Cylinder Testing: I've dripped water on each manifold runner to check and make sure they were hot after only a couple minutes of idle. All runners were hot (and presumably all cylinders functional).
Compression Testing: Previous compression tests showed good for all cylinders.
Engine Codes: none
As I mentioned I'm at my wit's end and desperate for potential solutions. Is it possible there could be some magical timing issue where the car runs fine but boost is retarded? Or some other issue with the engine itself that would inhibit the turbo from spooling, but otherwise appear to run quite well? I'm fairly certain it's not some sort of air/exhaust flow problem at this point. After a year of trying to solve this I'm about ready to give up on my Supra (even after all the work I've put into it). The only thing stopping me is that there has to be some sort of logical reason why it's doing this.
Please help!!
Thanks,
Jon
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