Hi everyone, i just rebuilt the top end of my 88 mk3 w/7mgte (Mods: D-motion FMIC D-motion egr block off kit) and i bought a new turbo from cx racing (ct26) (wich im starting to think was a mistake) when i first got it it was clocked wrong and i had to take it apart and reclock it so i could bolt it to the engine, on the first drive the boost gauge pegged past 10 psi on my aftermarket gauge. (wich is installed right) i found the flapper where the w/g actuator rod connects to it was hitting the stock downpipe on the casting protusion, i couldnt fit a grinder in there and it was bareley hitting so i bent it just a hair so it would open freely, still pegged past 10psi and wouldnt open, i loosened the actuator rod just so it had enough spring tension to keep the flapper closed, now it will go to7-10psi and spike or go past 10psi, even around 3k half throttle im boosting around 6psi. any input on what i should do? Ive been babying it since i know it has this problem. once i see the boost go to high i back off. i just need some input, im thinking the wastegate actuator may be bad from the get go. vacuum line to it is good. i dont have a pressure pump to test it with. thanks for any input.