Idle and miss issues

wolf1991

New Member
Apr 4, 2005
4
0
0
50
Ft Lauderdale, FL
Ok here's the deal. I just pulled my supra out of storage after sitting for 6 years or so. I have been systematically attacking the various systems. The fuel was obviously old so that was the first thing I changed along with the fuel filter. After that I found out that the fuel pump was bad so I changed that our with a Walbro unit. It cranked up after a few cranks but it would not idle and had a slight miss. I then pulled the plugs and checked them and the wires. Everything was in good working order, actually brand new condition. I checked the Idle Speed Control Valve and found that it didn't work when I applied power to the unit as specified in the TSRM. I ordered one from a member on here and installed it. I checked the TPS and found it to be within spec. I decided that it would be a good idea to have the injectors cleaned and tested. The injectors are freaking spot on. 447cc +-1 across the board. The miss only seems to be noticeable below 1500 rpm and it will not idle on its own. It runs like a champ all the way up to 5500 and boosts like it always did. Only upgrades are cat back and HKS intake. I've checked for codes multiple times and I have none. My next step will be to do a compression check and continue searching for a vacuum leak. If anyone has any suggestions please let me know.

Thanks, Jeremy

Cliff notes
Issue:
Runs rough below 1500 rpm and won't idle.
Items completed:
1. TPS checked
2. Injectors cleaned, checked, and matched.
3. ISCV replaced with working unit.
4. Fuel pump, filter, and fuel replaced.
5. Spark plugs and wires inspected (great condition).
6. No codes.
 

airhead04

New Member
Aug 21, 2009
1,489
1
0
Lima, Ohio, United States
Dont boost it anymore please. Just because it feels like its running good doesnt mean it is. If you have any air leask somewhere you may be going lean under boost. And a hole will find its way into your piston.
 

wolf1991

New Member
Apr 4, 2005
4
0
0
50
Ft Lauderdale, FL
I guess I should have said a HKS filter. Yeah you're right Airhead, I knew better than that. Hope all is well inside the motor. I took a peak down in the chambers but I really couldn't see much. I pulled the intake manifold today and found the gasket to be busted in multiple areas. I have no idea how it could have blown like that. Everything was tight. Hopefully it will run like its supposed to in a few hours.