So Ive been Daily driving my car with a boost controller set at 10psi and would occasionally hit fuel cut if I went passed half throttle. Got tired of fuel cut so I took out the boost controller and set it back to stock. I went for a little drive, did a small pull getting on the free way. Boost stayed at 8psi pulled pretty decent. As soon as I pulled off the car was misfiring horribly, sounded like a lawn mower. I limped the car home to find oil flooding the spark plugs in 5 and 6.
I figured that was the cause of the misfire so I cleaned out the oil and installed new plugs. Didn't change a thing. Car still ran like hell so I thought I should check the compression.
Results
160 140 152 160 65 62
The motor was built in 2010 .20 JE pistons, cometic HG with ARPs. Has less than 12K miles. I rarely beat on the car since it is my DD
The car doesn't smoke at all, never has. It has never over heated or ran low on oil. Do you guys have any ideas what it might be? I don't have a leak down tester or an air compressor..
I figured that was the cause of the misfire so I cleaned out the oil and installed new plugs. Didn't change a thing. Car still ran like hell so I thought I should check the compression.
Results
160 140 152 160 65 62
The motor was built in 2010 .20 JE pistons, cometic HG with ARPs. Has less than 12K miles. I rarely beat on the car since it is my DD
The car doesn't smoke at all, never has. It has never over heated or ran low on oil. Do you guys have any ideas what it might be? I don't have a leak down tester or an air compressor..