My issues began with a Lexus AFM question but have graduated to a whole different level, so thought it best to begin a new thread with a compilation of the process I have followed. Once again in-case anyone did not see the original thread, here is the link ( "http://www.supramania.com/forums/showthread.php?125196-Lexus-AFM-Clarifications-Please" ) and below are the list of mods and results of testing done in the last 48 hours:
1988 5spd 7mgte
Motor & tranny top to bottom complete re-build - Stock internals
Greddy 2.0mm MHG
ARP Head, Main & Rod Bolts
Upgraded oil pump (BP'd for higher flow)
Arizona Performance HF Oil pump hardpipe.
DM 57 Trim bolt-on upgrade
Synapse Engineering BOV recirculated with custom 1.5" nipple on intake
Alum 2.5" hardpipe & intercooler
AEM TruBoost
Apexi Neo
AEM Wide Band
Lexus AFM
Siemens 550cc injectors
AFPR
Denso MarkIV TT FP
Stage 3 Action clutch
Full 3" exhaust
Primary symptoms:
Missing during throttle run-up (not driving) and when driving. does ok under about 5% throttle then begins to start missing, more to do with manifold pressure or something not actual position of throttle.
The #1 spark plug was the only one turning black and would after a few minutes begin to foul, but with very little running time, i had a hard time telling if it was oil or gas issue. I could see an oily substance on the top of the #1 piston, all others looks clean. All other plugs were always clean, so my testing so far has been focused on #1
I did the following tests, not in this order, but based on following a path as I ruled out possible issues:
Compression Test at Operating Temp
#1 - 165
#2 - 165
#3 - 165
#4 - 167
#5 - 165
#6 - 170
Leak Down - I only did #1 and #2 so I have a comparison to one that did not appear to have any issues -
#1 - 10%
#2 - 12%
Pulled injectors, went to a specialty injector shop - had them do a flow test -
All flowed @ 559cc variance less than 2%
Fuel Pressure set @ 34lbs with vacuum
- CPS. rebuilt one from Halsupramk3, also replaced wiring back about 12" to rid harness of any corroded wiring that was found, no change when manipulating the wires going into CPS.
- TPS - re-calibrated last week , had a different issue with a serious stumble and it went away after resetting, also tested via code 51 when I just barely touch throttle pedal.
- Ingnitor - tested per TRSM - passed (including the 3vdc testing process)
- Coil Pack - tested per TRSM - passed
- Resistor Pack - tested per TRSM passed
- O2 sensor - tested using the mVA ratings per TRSM, seemed normal after EGTs got passed 600
- Changed all spark plugs - they are gap'd at .28
- Checked resistance of ignition wires - MSD8.5, also tried changing back to stock ones
- Switch far left coil pack for far right coil pack - issue did not follow
- Checked for any arcing by turning all lights off in shop so that is was pitch black - rev'd up motor, two of us watching from either side of car, no visible arcing
- Checked all grounds - I also adding additional grounding with a termination wheel at the battery (6awg wire), I added them to valve cover, alternator, plenum, another location on block.
- Was suspicious of vacuum leak, so took plenum and intake off, bought new gaskets, checked all surfaces, carefully put all back together, but no change on start-up. but the lower gasket was moist around #1 chase all the way the the atmosphere, the others were a little moist around chase opening, but only like 1/4". But this lower one was part of the kit, was a little cheesy so was glad to get better gaskets anyway for those pieces.
- Last test, not sure how accurate, but used a timing light while revving engine, to see if the missing was coming from the ignition side or the fuel side... seemed obvious to me that the light would be following when it would miss. #1 and #6 seemed to be the worse (which makes some sense since they are on the same coil pack, yet I switched them and problem did not follow pack) yet I was getting some misses in light on all of the wires I tested... No missing then coming down to idle (let off throttle) Not sure if a timing light can really keep up with that though??
I am also wondering if the missing is happening on all of the cylinders randomly, but there was some oil in #1 and #6 after initial runs to get everything seated in, so 1st set of plugs, #1 and #6 were black, others clean, next set of plugs #6 was clean now, but #1 black, but also now #6 piston had no visible residue, where the #1 still did, so wondering if that just made it worse for that one, as when it missed, it would also have oil or something thrown at it, so it would foul faster between the combination of the two issues at once.
Still no codes at this time, have had zero codes thrown since start-up.
I know that was a lot, but I want it to be clear that I have checked everything I could think of to check (so asking for help, not asking to be spoon fed lol)... Any and all ideas would be appreciated, even if they are far fetched (CajunKenny, that does not include you, as my flux-capacitor is working just fine :icon_bigg)
Thanks!
1988 5spd 7mgte
Motor & tranny top to bottom complete re-build - Stock internals
Greddy 2.0mm MHG
ARP Head, Main & Rod Bolts
Upgraded oil pump (BP'd for higher flow)
Arizona Performance HF Oil pump hardpipe.
DM 57 Trim bolt-on upgrade
Synapse Engineering BOV recirculated with custom 1.5" nipple on intake
Alum 2.5" hardpipe & intercooler
AEM TruBoost
Apexi Neo
AEM Wide Band
Lexus AFM
Siemens 550cc injectors
AFPR
Denso MarkIV TT FP
Stage 3 Action clutch
Full 3" exhaust
Primary symptoms:
Missing during throttle run-up (not driving) and when driving. does ok under about 5% throttle then begins to start missing, more to do with manifold pressure or something not actual position of throttle.
The #1 spark plug was the only one turning black and would after a few minutes begin to foul, but with very little running time, i had a hard time telling if it was oil or gas issue. I could see an oily substance on the top of the #1 piston, all others looks clean. All other plugs were always clean, so my testing so far has been focused on #1
I did the following tests, not in this order, but based on following a path as I ruled out possible issues:
Compression Test at Operating Temp
#1 - 165
#2 - 165
#3 - 165
#4 - 167
#5 - 165
#6 - 170
Leak Down - I only did #1 and #2 so I have a comparison to one that did not appear to have any issues -
#1 - 10%
#2 - 12%
Pulled injectors, went to a specialty injector shop - had them do a flow test -
All flowed @ 559cc variance less than 2%
Fuel Pressure set @ 34lbs with vacuum
- CPS. rebuilt one from Halsupramk3, also replaced wiring back about 12" to rid harness of any corroded wiring that was found, no change when manipulating the wires going into CPS.
- TPS - re-calibrated last week , had a different issue with a serious stumble and it went away after resetting, also tested via code 51 when I just barely touch throttle pedal.
- Ingnitor - tested per TRSM - passed (including the 3vdc testing process)
- Coil Pack - tested per TRSM - passed
- Resistor Pack - tested per TRSM passed
- O2 sensor - tested using the mVA ratings per TRSM, seemed normal after EGTs got passed 600
- Changed all spark plugs - they are gap'd at .28
- Checked resistance of ignition wires - MSD8.5, also tried changing back to stock ones
- Switch far left coil pack for far right coil pack - issue did not follow
- Checked for any arcing by turning all lights off in shop so that is was pitch black - rev'd up motor, two of us watching from either side of car, no visible arcing
- Checked all grounds - I also adding additional grounding with a termination wheel at the battery (6awg wire), I added them to valve cover, alternator, plenum, another location on block.
- Was suspicious of vacuum leak, so took plenum and intake off, bought new gaskets, checked all surfaces, carefully put all back together, but no change on start-up. but the lower gasket was moist around #1 chase all the way the the atmosphere, the others were a little moist around chase opening, but only like 1/4". But this lower one was part of the kit, was a little cheesy so was glad to get better gaskets anyway for those pieces.
- Last test, not sure how accurate, but used a timing light while revving engine, to see if the missing was coming from the ignition side or the fuel side... seemed obvious to me that the light would be following when it would miss. #1 and #6 seemed to be the worse (which makes some sense since they are on the same coil pack, yet I switched them and problem did not follow pack) yet I was getting some misses in light on all of the wires I tested... No missing then coming down to idle (let off throttle) Not sure if a timing light can really keep up with that though??
I am also wondering if the missing is happening on all of the cylinders randomly, but there was some oil in #1 and #6 after initial runs to get everything seated in, so 1st set of plugs, #1 and #6 were black, others clean, next set of plugs #6 was clean now, but #1 black, but also now #6 piston had no visible residue, where the #1 still did, so wondering if that just made it worse for that one, as when it missed, it would also have oil or something thrown at it, so it would foul faster between the combination of the two issues at once.
Still no codes at this time, have had zero codes thrown since start-up.
I know that was a lot, but I want it to be clear that I have checked everything I could think of to check (so asking for help, not asking to be spoon fed lol)... Any and all ideas would be appreciated, even if they are far fetched (CajunKenny, that does not include you, as my flux-capacitor is working just fine :icon_bigg)
Thanks!
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