I took my car to a performance shop to have them program my new AEM ECU and to tune it. They got the car started and idling great but then on the dyno it started to push coolant but they said that it never overheated (they shut it down in time). They said that they weren't boosting at the time (had boost at 0 during the initial runs). Claimed that the car still ran afterward, albeit pushing coolant and running rough - they thought that a cylinder or two may not firing.
I had it towed to another mechanic to have him diagnose and fix the problem (the performance shop said that they wouldn't do the engine work). He couldn't get the car started and couldn't figure out why. The performance shop claimed that it started with no problems before I towed the car. The mechanic couldn't find any problems so he removed the head and found that all the cylinder walls had scuffing and striping. The scuffing is worse on the exhaust side. He also said that the block is bowed straight down the middle, lengthways, between each piston. It's a small valley but large enough to not allow a MHG to seal. However, the head checked out ok - no warpage. He said that the MHG looked ok too. Said that the head studs were not loose.
I need to get this repaired but I'm asking for opinions on what may have happened here. The mechanic says that he doesn't understand how and when it failed. He thinks the scuffing may have occurred over time but the striping, warped block, and supposed gasket failure is a mystery. His initial thoughts are either the machine shop did poor work on the block (they installed the pistons and rods too) or there was an extraordinary heat event that caused this damage.
A little background on the engine:
completely rebuilt about 6,000 miles ago and ran great up until this point. The rebuild consisted of many things including:
- JE pistons 84MM bore (purchased from Reg Reimer w/ his custom spec's: offset pin, 10 thou raised pin, dropped 1st and 2nd ring land, stronger lands, chamfered skirt)
- Toyota piston rings
- ARP head studs, rod bolts, mains
- stock rods
- 1MM oversize valves
- head and block tested, machined, blueprinted.
- Cometic 1.5MM MHG
- Stock Toyota ECU w/ Apexi SAFC2 and Greddy boost controller
- 550 injector / lexus AFM mod.
- walbro fuel pump, Aeromotive AFPR.
- car was tuned by a shop on a dyno.
Then I upgraded a few things before this recent tune (car was not running after these upgrades - I had it towed to the performance shop for them to program the AEM and tune it):
- AEM ECU
- removed AFM, installed MAP sensor
- SupraSport BOSS turbo
- 850cc siemens injectors from Driftmotion
- ATI super damper
- rewired injectors for sequential ignition and did the DH61 ignitor mod.
- PLX wideband and EGT sensors
Attached are pics of the block (head pics in the following post).
Anyone think they know what caused this? Thanks.
I had it towed to another mechanic to have him diagnose and fix the problem (the performance shop said that they wouldn't do the engine work). He couldn't get the car started and couldn't figure out why. The performance shop claimed that it started with no problems before I towed the car. The mechanic couldn't find any problems so he removed the head and found that all the cylinder walls had scuffing and striping. The scuffing is worse on the exhaust side. He also said that the block is bowed straight down the middle, lengthways, between each piston. It's a small valley but large enough to not allow a MHG to seal. However, the head checked out ok - no warpage. He said that the MHG looked ok too. Said that the head studs were not loose.
I need to get this repaired but I'm asking for opinions on what may have happened here. The mechanic says that he doesn't understand how and when it failed. He thinks the scuffing may have occurred over time but the striping, warped block, and supposed gasket failure is a mystery. His initial thoughts are either the machine shop did poor work on the block (they installed the pistons and rods too) or there was an extraordinary heat event that caused this damage.
A little background on the engine:
completely rebuilt about 6,000 miles ago and ran great up until this point. The rebuild consisted of many things including:
- JE pistons 84MM bore (purchased from Reg Reimer w/ his custom spec's: offset pin, 10 thou raised pin, dropped 1st and 2nd ring land, stronger lands, chamfered skirt)
- Toyota piston rings
- ARP head studs, rod bolts, mains
- stock rods
- 1MM oversize valves
- head and block tested, machined, blueprinted.
- Cometic 1.5MM MHG
- Stock Toyota ECU w/ Apexi SAFC2 and Greddy boost controller
- 550 injector / lexus AFM mod.
- walbro fuel pump, Aeromotive AFPR.
- car was tuned by a shop on a dyno.
Then I upgraded a few things before this recent tune (car was not running after these upgrades - I had it towed to the performance shop for them to program the AEM and tune it):
- AEM ECU
- removed AFM, installed MAP sensor
- SupraSport BOSS turbo
- 850cc siemens injectors from Driftmotion
- ATI super damper
- rewired injectors for sequential ignition and did the DH61 ignitor mod.
- PLX wideband and EGT sensors
Attached are pics of the block (head pics in the following post).
Anyone think they know what caused this? Thanks.