due to some issues we are having with a friends car. can you use a 89 ecu on say a 90, or 91, 92 etc.. engine harness? the harness he bought is supposed to be an 89 harness. but idk. we have tried 3 diff ecu's that are all supposed to be 89 ecu's,. and same problem. it breaks up really bad under boost.
it is a stock rebuilt 7mgte with mhg and arp's, stock ct26. fmic with 2.5in piping. no vac leaks at all. this is in a toyota pickup. we have tried known good parts from my 7mgte when it was on stock electronics. have tried cps, coils, ignitor, tps, coolant sensor, cold start switch, 3 diff ecu's as mentioned before. another afm, etc... it seems to be running pig rich. smells like it anyway. im lost at this point as the ecu is throwing no codes at all. we even used a voltage tester on the engine harness plug itself thinking somehow the enging light wiring was wrong. no codes. runs and idles smooth. just when driving it breaks up bad. timing is at 10deg. cam timing is perfect. had him regap the plugs from stock gap of 32 thousandths to 28. same, no change. its all stock except the i/c, pipes, and 3in downpipe.
anyone got any ideas/ all i can think of is its an issue with the harness not being an 89 like it was supposed to be or something.
it is a stock rebuilt 7mgte with mhg and arp's, stock ct26. fmic with 2.5in piping. no vac leaks at all. this is in a toyota pickup. we have tried known good parts from my 7mgte when it was on stock electronics. have tried cps, coils, ignitor, tps, coolant sensor, cold start switch, 3 diff ecu's as mentioned before. another afm, etc... it seems to be running pig rich. smells like it anyway. im lost at this point as the ecu is throwing no codes at all. we even used a voltage tester on the engine harness plug itself thinking somehow the enging light wiring was wrong. no codes. runs and idles smooth. just when driving it breaks up bad. timing is at 10deg. cam timing is perfect. had him regap the plugs from stock gap of 32 thousandths to 28. same, no change. its all stock except the i/c, pipes, and 3in downpipe.
anyone got any ideas/ all i can think of is its an issue with the harness not being an 89 like it was supposed to be or something.